October 9th 1916

Hands called at 4.0 AM and changed (?) into coaling rig straight away. Worked main derreck, out ladders etc when hands fell in and started
coaling about 6.0 AM. Took in 980 tons from “Frances Duncan”. Finished about 10.30. Cleaned ship etc. afterwards. Rotten wind blowing, rianing &
very cold. Make & mend in afternoon. Went to see Lieut. Harrison re Motor Boat Reserves.

October 9th 1916

October 9th 1916

October 9th 1916 B

October 9th 1916 B

October 7th 1916

Ordinary Routine before breakfast. Got under way about 9.0. a,m, Wnt to Divisions and Action Stations directly afterwards. Fired 13.5 3/4 charge.
6 rounds per gun. Kept YAW Record in lower conning tower. Returned to anchorage about 11.30. Had to scrub decks again as hook was dropped as C in
C was coming on board in the afternoon. Make & mend in afternoon. Got head down. Got under way about 6.30 for Return trip. Had first Watch. 

October 7th 1916

October 7th 1916

October 5th 1916

Got under way about 8 o’clock and dropped hook about 8.45. 4″ day action crews did 1″ aiming in forenoon. Saw Captain re: Motor Boat Reserve. Not
very cheering news as they want men who have had a certain amount of experience. Said he’ll write again to Admiralty and recommend us for
consideration. Painting in 4″ Flat in afternoon. Starboard Watch on fos’cle from 4.30 until 6.45 working cable, although watch below. Got under
way about 4.30. Sub Caibre firing. Night defence at 6.30. White Watch stand fast. Fired 4 rounds per gun, 2 runs.

 October 5th 1916


October 5th 1916

October 4th 1916

Diving party for cable first thing. Got gear in boat before breakfast. Got under way about 7.45 and went to calibrating ground. Washed out of
diving party after breakfast. Told off to see Captain in forenoon but nothing doing owing to calibration. Calibrating 13.5’s in forenoon and part
of afternoon. Working over side painting all day. Got under way about 3.0 p.m. and went over to place where we had dropped anchor. Diving party
had found same and shackled on 4″wire. 2nd part of Starboard on fos’cle after tea to get anchor in, but wire was not large enough and so dropped
buoy until the morning. Went back to anchorage about 6.0 p.m.

October 4th 1916

October 4th 1916